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http://www.fortmcmurraytoday.com ... -and-pipeline-spill
, x% K: |; r* q2 `! {( i+ b. YNexen Energy will lay off about 350 workers from its Long Lake facility, following its release of results of internal investigations into a July 2015 pipeline spill and the January 2016 hydrocracker explosion.
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# f# b3 G0 A' yThe CNOOC-owned energy company will only be continuing its steam-assisted gravity drainage (SAGD) operations at Long Lake, after it determined a short-term repair was not possible for the hydrocracker unit, which killed two employees when it exploded on Jan. 15, 2016.
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8 H( z, M8 G; u6 N5 T. }: E1 [, [The facility's upgrader has been idling since then, and will be moved into winter preservation, with no estimation of when it will be brought back into service.
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* `* I. T6 ~6 _0 iAn internal investigation found the explosion was a result of work being performed that was "outside of the scope of approved work activities."
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! P1 ~ K& E3 |/ V) v! lThe two employees killed, both Fort McMurray residents, were 52-year-old Drew Foster and 30-year-old Dave Williams. Foster was killed in the explosion. Williams, who was flown to the University of Alberta Hospital's burn unit hours after the explosion, died a week later.
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In its announcement Nexen said it is addressing safety gaps in part with refresher training on workplace hazard identification, increased site supervision and safety inspections. ) Y/ [# y Z( R' b
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The decision to move to a SAGD-only operation was described as "entirely economic," and will result in about 350 staff layoffs, most of which will be completed by the end of 2016.
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; H2 S, H0 P0 t" P2 CThe results of the investigations were given at a news conference on Tuesday by Nexen CEO Fang Zhi and Senior Vice President of Canadian Operation Ron Bailey.
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9 R/ F% @7 l {- uNexen also said it found the root cause of a July 2015 emulsion spill at Long Lake to be a "thermally-driven upheaval buckling of the pipeline, and the subsequent cooldown during the turnaround."3 G7 e2 c: K) y- ]
7 a7 x0 R9 ]# {" J! \8 ^This was caused because of pipeline design incompatible with the muskeg ground conditions, and steps that could have been taken to mitigate the potential for buckling were not addressed. 5 k/ v9 v# d2 f( J7 D* U+ S" [
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The spill poured up to five million litres of emulsion - a mixture of water, bitumen and sand - into surrounding muskeg. The spill may have been ongoing for up to two weeks when it was discovered in July 2015 by a contractor walking through the area.
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In August the Alberta Energy Regulator ordered Nexen to shut down 95 pipelines until the company could prove the pipelines could be operated responsibly. The suspension was lifted in September 2015.
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- with files from Vincent McDermott |
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